Objetivo Application of technology involving microprocessors and digital type control loops for optimum process performance of blast furnace hot stoves with waste heat recovery system and ceramic burners.The regulation and reduction system of rich gas (coke oven gas or natural gas) started with a short delay due to seal problems of the adjusting throttle. The realization of the "supervision and optimization through process computer" was not on time due to problems affecting both the hardware and the software faced during the phase of the micro dialogues. The experimental verification of the model was showing some problems owing to the difficulty of availability of reliable measures when the operational parameters change.Today the system is full in operation.First significant historical data could be presented. Prints and graphic diagrams as supplied by the process computer showed the trend of the most significant variables. The 3 years results show an improvement in the plant efficiency: about 1%.The plant operation will be governed by a microprocessor which will regulate directly the valve and the control loops to optimize rich gas consumption (in mixed gas combustion system). The process control computer (via teleprocessing) will communicate with the microprocessor for the supervision and optimization of the process. Programa(s) ENG-ENALT 1C - Programme (EEC) of financial support for projects to exploit alternative energy sources, 1979-1984 Tema(s) 1.6 - INDUSTRY Convocatoria de propuestas Data not available Régimen de financiación DEM - Demonstration contracts Coordinador Nuova Italsider SpA Aportación de la UE Sin datos Dirección Via Corsica 4 16128 Genova Italia Ver en el mapa Coste total Sin datos